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Issue with StanfordDoggoOuterBigPulley.stl.step #37
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Allows fast cloning of 3DP artefacts. Enables Git/PR workflow for revisions to these artefacts. Solves issue Nate711#37. Files live in `/DoggoHardware/3D Printed`. Folder does not distinguish between FDM and SLS parts. Tracks new 3d printed parts, which should be added to BOM: 1. Pulley Bracket 2. Inner Shaft Spacer
Allows fast cloning of 3DP artefacts. Enables Git/PR workflow for revisions to these artefacts. Solves issue Nate711#37. Files live in `/DoggoHardware/3D Printed`. Folder does not distinguish between FDM and SLS parts. Tracks new 3d printed parts, which should be added to BOM: 1. Pulley Bracket 2. Inner Shaft Spacer
@ulaladungdung, @methylDragon, see my feature branch for fresh STL and STEP files: These include all 3d printed parts in project. I've generated them directly from the fusion 360 model, and double checked them. |
Notes:
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Hi @maxsu Thanks so much for the help!! And yes please, the revision would be amazing as we already have the A333 on hand. Cheers!! |
See the updated stl. Fusion version is here. Be careful; I increased the minimum wall thickness by 15% (to 1.15mm), but the insert's centerline could drift during heated installation. Let me know if you need a heavier revision. @Nate711: |
Our robot uses the A310 screw-to-expand inserts but that caused an issue where if you really tighten the set screws that go inside of the inserts and then try to unscrew those set screws, the A310 insert sometimes spins inside the plastic instead of allowing the set screw to unscrew. |
Hi!! Thanks for sharing the doggo project to the public. My team is currently facing difficulty in printing
StanfordDoggoOuterBigPulley.stl.step
as the file appears to be corrupted. Do you have any advice regarding this?I used the download link from the shared BOM
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