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Bugs - to be fixed in the next commit. Z-limit has to be polled since it has the same pin number as X preventing enabling interrupt handling for it. #103
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Now Homing in XYZ axes still works when "$H" is sent. But all the three hard limit switches in the XYZ axes can't be triggered. |
All three works for me for triggering hard limit alarm. Did you forget to enable hard limits with $21=1?
Oops, a regression. This line https://github.com/grblHAL/core/blob/bf6823abf91986bc840e5e9497ed9b861000b5d8/motion_control.c#L891 should be
I'll commit a fix later (will be a few days). |
I did enable hard limits with Settings: Grbl, otherwise the homing would not work. Just sent "$21=0" and "$21=1" with MDI input, weird that there was no response (the Settings: Grbl were not changed). BTW, is it possible to send the grbl commands in a CNC file? Thank you for your help. |
| But all the three hard limit switches in the XYZ axes can't be triggered. | All three works for me for triggering hard limit alarm. Did you forget to enable hard limits with $21=1? | I did enable hard limits with Settings: Grbl, otherwise the homing would not work. |Just sent "$21=0" and "$21=1" with MDI input, weird that there was no response (the Settings: Grbl were not changed). Sorry, my bad. I mixed homing enable up with hard limit enable. All three work now for triggering hard limit alarm. And $21=1 works as well. |
| https://github.com/grblHAL/core/blob/bf6823abf91986bc840e5e9497ed9b861000b5d8/motion_control.c#L891 |should be |homed_status = limits_go_home(cycle); Changed this line as suggested and rebuilt. The homing in Z axis failed with alarm 8 even if I increased the pull-off setting to 10mm. The XY axes completed homing with 10mm pull-off. |
Originally posted by @terjeio in #99 (comment)
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